From SolidWorks to Delrin
After the informative and experience filled process of
modeling our bottle opener on SolidWorks, we were finally ready to print a 2-D
DXF copy on the laser cutter. For this task we selected a 1/8'' thick
Delrin sheet and began the process of learning how to use the laser cutter. Or
at least that’s what we thought would happen…
When it got down to actually uploading our design to the
printing software, Corel could not read our file completely. We thought the
lack of some lines in our design was an error in the saving process, but after
multiple trials going to and from computers, this did not seem to be the case.
Eager to see if the design actually functioned, however, we decided to just
print out our model in its most basic state and worry about its aesthetic
elements later.
With our design all printed came the moment of truth. Would it work? Did we have to choose another design? Turns out......
It worked!
Over the course of the week we worked a lot with Larry, our
machinist, sorting out the printing trouble we had on the first day. Thanks to
his help we were able to print out our first full model, tentacles and all!
Our work was not done here though. It turns out that we
still had a lot of things to lean about what not to do when using the laser
cutter.
Trial 1: Bottle Opener/knife
Starting from this
point on, Vicki and I decided to use a 3/16" sheet of Delrin. At first I
was confused about where this pointy protrusion had come from, but it turns out
Vicki had added it to see if it could aid in the bottle opener’s
function. She thought it could be used
to pry open the bottle cap in some way.
The main reason we moved on from this trial, however was
because our dimensions were slightly off. Despite making an effort to check the
dimensions and measure some of the parameters by hand, we learned that we
needed to use SolidWork’s "Measure" function for the design to truly
work out .
Trial 2/3:
When we printed out this final version of the jellyfish
design, our dimensions were finally correct. It was the perfect size for the
hand, and it made contact with the bottle cap in all the places it was supposed
to. Only… it just would not open the bottle.
We tried filing the straight edge of the opener to make it fit
under the cap more easily, but this did not work. Finally, we came to the
conclusion that the curve of the head was too narrow for applying force the way
we wanted it to. In this case, the action of the bottle opener relied on having
a force applied tangent to force of the straight edge lever, and this just
wasn’t occurring.
Rather than continue with this design, we decided it was
time to move on.
This thread of posts was really interesting to read. I really like how you laid the sections out in your posts, distinguishing the steps you took with descriptions, visuals, and ideas you had along the way. Your sketches were very impressive and the evolution from sketch to jellyfish prototype to bee was fun to see. Your posts clearly explain your thought process while also making them enjoyable to read. I especially like how you acknowledged Larry's help along the way. I'm glad your bottle opener was successful!
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